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Change Order 08_ALSC-Contractor Signed
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2026-06-02 10:00 AM - Commissioners' Agenda
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Change Order 08_ALSC-Contractor Signed
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Last modified
5/28/2026 12:29:13 PM
Creation date
5/28/2026 12:26:23 PM
Metadata
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Template:
Meeting
Date
6/2/2026
Meeting title
Commissioners' Agenda
Location
Commissioners' Auditorium
Address
205 West 5th Room 109 - Ellensburg
Meeting type
Regular
Meeting document type
Supporting documentation
Supplemental fields
Item
Request to Approve Change Order #8 for the Ellensburg Rodeo Arena Project
Order
13
Placement
Consent Agenda
Row ID
144971
Type
Contract
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Selland Construction Prevailing <br />Job Name: Ellensburg Rodeo Arena Improvements Job Code: 2550-30 <br />Cost Code Review <br />Cost Code: 98-005 T&M: Overexc. & Rock Placement F TN <br />Code Description Class Reg. Hours OT Hours Other Hours <br />Printed on: 03/05/2026 10:49:34 <br />x__________________________________________ Date: ______________ <br />Attendance/Non-Use Codes included in Hours: None / None Page 5 <br />Date: 12/18/2025 Foreman: 2566 Shift: 1 <br />Time Card: <br />Production Quantities: 0.000 <br />2347 ANTONIO SISCO 350 0.50 0.00 0.00 <br />LD363 2012 CAT 930H Loader 0.50 0.00 0.00 <br />1192 JOSHUA SAMPSON 210 1.50 0.00 0.00 <br />2541 PARKER BERMAN 310 1.50 0.00 0.00 <br />BH354 2021 Komatsu PC238 Exc 1.50 0.00 0.00 <br />2566 DYLAN BROWN 810 0.50 0.00 0.00 <br />Labor Totals: Hours - 4.0 <br />Equip Totals: Hours - 2.0 <br />Cost Code Notes: <br />Slot:2 <br />Company Note: <br />Indexes: <br />Inspector Note:There was an engineering error on depths on an already dug footing the had already had a .5 over excavation don't in the spread <br />footing location. With was already at the groundwater depth it was a f9.5 footing callout and the depth of bottle. Of footing was <br />1568.00 which was about .75 below the water table. <br />This build was an error on the engineers behalf and really should have been a bottom of footing at 1569.5. <br />This was all built up with base course and compacted in. <br />This task took a hour <br />The other half hour on this days T&M was the amount of time to over excavate the east building continues footing locations in <br />between the spread footings. <br />The continues footing on this building stays about .75 higher then the spread footings. In this separations of elevations between the <br />two builds is the difference of the spread footings being on a non yielding surface and the continues footing wall being on a yielding <br />surface beyond what would pass for a stable base. Over excavation is essential into getting our stable non yielding base to build on.
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